Friday, February 12, 2016

Red Logitech Momo Force Hub Repair Method and 3D Printed Replacement


The hub of my red Logitech Momo Force that I’ve owned since 2003 broke last week.  A replacement part is not available.  I came up with a repair method that can also reinforce unbroken hubs. 

I have not tested the repaired hub yet, because while I was measuring it to design a 3D model for my friend’s 3D printer, I found a completed 3D printable hub model by user StoraBrollan on thingiverse.com.  I forwarded his model to my friend to look at and continued working on my own 3D model, because I wanted to include my reinforcement.  Then my friend texts me that he went ahead and printed StoraBrollan’s hub.  Link to StromBrollan's replacement hub 

With a little work to correct ABS shrinkage on my friend's printer, StromBrollan's hub design is installed and working.  I designed another 3D printable part to add my reinforcement to his 3D printed hub.  My part also keeps the steering angle limiter aligned if the hub breaks in the same place again, to protect the wheel angle sensor from over rotation.  Link to spacer  

Repair/Reinforce Method

The force feedback gear is held onto the hub with 3 internal m3x20mm screws that thread into an external metal ring.  The hub breaks just past the screw heads because that center section has to transfer all of the gear torque to the steering wheel.  My hub had a crack almost all of the way around.  It didn’t crack all the way because I finally checked it after hearing a loud crack and realizing the wheel could tilt. 
The force feedback gear and threaded metal ring slide onto the hub from the outside, and are held on with screws from the inside. 
Large end of hub with internal ledges, the force feedback gear screws go into the 3 hole pattern deep inside.  The hub eventually breaks just above them.

The large opening of the hub has inner ledges.  I drilled and carved a metal washer with a rotary tool and metal files until it would sit on the ledges.  Three notches have to be made to fit around the pockets that prongs on the steering wheel mounting ring fit into from below.  These pockets and notches help because they prevent the washer from turning.  Now longer m3x45mm screws can replace the 20mm screws holding on the force feedback gear, and clamp the hub back together. 

http://i696.photobucket.com/albums/vv325/wrlin00/IMG_2407a.jpg
Threaded gear mounting ring, PVC spacer, notched washer, and m3x45mm screws

I made a spacer to hold the m3x45mm screws straight, by sanding a piece of 3/4" PVC pipe to fit inside a 1” PVC pipe, gluing them together with PVC cement, and cutting slots.  This will hopefully allow the screws to transfer some torque between each other to the notches of the washer, instead of all of the torque going through the hub center section and cracking it again.  The spacer needs a gap under the notched washer so that the washer can provide a clamping load on the hub, my spacer thickness was about 18mm.  A spacer could also be made with no sanding or gluing from a 1”x1/2" PVC bushing, I just didn’t want to go to the hardware store.  Or the spacer could be 3D printed.
Hub with spacer for holding longer screws straight
Hub with spacer, notched washer, and longer screws
http://i696.photobucket.com/albums/vv325/wrlin00/IMG_2408a.jpg
Repair components assembly


I also glued the crack with ABS pipe cement, and used my repair method to clamp it while the cement set.  The small end of the hub was also cracking where the wheel angle sensor fits, so that also got ABS cement and metal foil tape.

http://i696.photobucket.com/albums/vv325/wrlin00/IMG_2434a.jpg
Additional repair materials
If the cracked section of hub broke into pieces instead of forming a crack, it might be possible to cut it out completely, make a new center section, and bolt it all together with my repair method.   In that case I might want to run the screws in the other direction so I could fasten them with 3mm hex nuts.  I also might drill everything out to use fatter m4x45mm screws and nuts.


3D Printed Replacement Hub


My friend printed the hub in ABS, which can have more shrinkage than the PLA that StromBrollan used.  This may have caused the tiny <1mm loose fit at the bearing and gear contact areas.  To see if the part would work anyway, I used layers of metal tape to build up these contact areas.  The gear keyways had to be shaved a little wider, and the edges of the cone holes had to be shaved for the gear mounting ring to lie flat.  PLA has less shrinkage and better layer adhesion than ABS, but ABS can be tougher, less brittle, and can be carved after printing.  I currently have no preference.


http://i696.photobucket.com/albums/vv325/wrlin00/20160209_152628a.jpg
3D printed hub with metal tape to build up contact surfaces

http://i696.photobucket.com/albums/vv325/wrlin00/20160209_152713a.jpg
Force feedback gear installed


3D printed hub screwed to steering wheel, the steering angle limiter protrudes from the metal mounting ring

My notched metal washer fits in the 3D printed part too, but longer m3x50mm screws are now needed to reach the gear mounting ring, because a ramp of material to aid 3D printing covers the shapes the notches used to mate with.  My local Ace Hardware store had both 45mm and 50mm m3 metric screws.  Those shapes only protruded because the injection mold designer removed as much plastic from the hub as possible to save money, which we're not concerned about anymore.  My own preliminary hub design on thingiverse is nearly solid and needs some hollowing out and 3D printing overhang ramps, and is actually more suitable for machining than printing.  The washer might be able to turn now, so the 3D printed spacer I designed might not transfer as much torque through the 50mm screws to the washer/hub interface, but it will still keep the steering angle limiter on the steering wheel mounting ring aligned if the hub breaks in the same area as before, to protect the wheel angle sensor from over-rotation.    
Link to 3D printable spacer 

Test fit
Test fit


Big thanks to StromBrollan and my friend with the 3D printer.






1 comment:

  1. Thank you for sharing. My beloved Momo Red wheel, bought 3 years ago from the original owner, recently made the dreaded crack sound and became a bit too mobile. I managed to find another on eBay for peanuts and this lasted for a month before its plastic hub also fractured. I have followed your approach using ABS cement, plastic spacers, longer hex bolts and have fabricated grooved washers from 2mm aluminium sheet. What a labour of love! Both wheels have also had Loctite applied to the motor screws, so they should hopefully outlast me. Thanks again for helping me to preserve these excellent FFB wheels.

    ReplyDelete